This one has me stumped. My 1987 Husky 238 that I fixed up from an ebay win is giving me headaches. Basically it will not idle at anything less than ~3200 rpm but it is spec'ed to idle at 2700. And when I give it full throttle, it makes a lot of smoke (I run 40:1 93 octane gas with Husky premium oil) like it is too rich and the sparkplug is very black. In addition, the high adjust screw seems to make little difference, even when screwed all the way in.
I did a top end rebuild using the original piston and cylinder. I replaced the crankshaft seals, ring, wrist pin bearing, gaskets, rebuilt the carb, replaced the the air filter, gas tank breather, the gas line, the gas filter and added a new NGK plug. Everything else was cleaned up to a fairly spotless state.
It has 165psi compression. I have pressure and vacuum tested it three times and it always holds 10psi / 10"h2o for minutes. And I do pull the starter cord while doing this.
I have replaced the carb with a known good one and replaced both the coil and the electronic module with known good ones. Neither helped.
I thought I was on to something when I found the carb pop-off pressure was 20+ pounds on the original carb but fixing that did not change anything. It uses a Walbro HDA-34A carb, and I have adjusted the metering lever so that it is flush with the carb body. And as I said above, another carb acts the same way.
I visually checked the manifold block and it looks ok. I plan to do a pressure test with the block in place just to be sure.
I removed the gas filter and did a pressure test on the gas line to the carb and it was fine. I ran it without an air filter - no difference. I ran it with the gas cap cracked open - no difference.
So, as I said, I am stumped. What am I missing?
I did a top end rebuild using the original piston and cylinder. I replaced the crankshaft seals, ring, wrist pin bearing, gaskets, rebuilt the carb, replaced the the air filter, gas tank breather, the gas line, the gas filter and added a new NGK plug. Everything else was cleaned up to a fairly spotless state.
It has 165psi compression. I have pressure and vacuum tested it three times and it always holds 10psi / 10"h2o for minutes. And I do pull the starter cord while doing this.
I have replaced the carb with a known good one and replaced both the coil and the electronic module with known good ones. Neither helped.
I thought I was on to something when I found the carb pop-off pressure was 20+ pounds on the original carb but fixing that did not change anything. It uses a Walbro HDA-34A carb, and I have adjusted the metering lever so that it is flush with the carb body. And as I said above, another carb acts the same way.
I visually checked the manifold block and it looks ok. I plan to do a pressure test with the block in place just to be sure.
I removed the gas filter and did a pressure test on the gas line to the carb and it was fine. I ran it without an air filter - no difference. I ran it with the gas cap cracked open - no difference.
So, as I said, I am stumped. What am I missing?