Wild Knight
ArboristSite Guru
I have had this project in the works for some time now. I have been learning a lot from Erick about theories on what makes chainsaws works, as well as what makes them work better. With Brad's and Slinger's ported 441's out there, we decided it was time to get off the pot. We decided to do a nice, basic woods port on my 441. We got together, took it apart and stared at the jug with the extra split transfer ports for a good long while. This definitely helped
Compression was OK. It was 155 pounds cold. Squish band was 0.0295", which isn't too hateful.
We got the jug off and checked the numbers.
Bore: 50 mm
Stroke: 36 mm
Exhaust opening: 96 degrees (168 duration)
Transfers opening: 125 degrees (110 duration)
Intake opening: 80 degrees (160 duration)
I have a good buddy up in Cincinnati. He is a fantastic machinist, as well as a big fan of fat-bottomed girls. We made a trip up to see him and he promptly milled the jug down 0.0295" and made a 0.020" pop-up for the piston. This brought our squish down to 0.020 and brought up the compression nicely. Also, the jug itself was not square to the crank case. It was off by a few thousandths on the axis of the hinge pin, causing the piston to rock slightly every time it went up and down. Nik, of course, corrected this flaw from the factory. Now things are tight and moving in alignment. Andre, Mike and Brad made it a point to stop by, and we had a mini-GTG just shooting the bull while everyone got pop-ups made.
Nik (FATGUY)
Jug and Piston:
Andre (Andyshine77) and Erick (Erick) shootin the bull (Sorry Mike, I didn't get any pics of you and your lovely bride):
Brad (blsnelling) excited about his new pop-up:
Compression was OK. It was 155 pounds cold. Squish band was 0.0295", which isn't too hateful.
We got the jug off and checked the numbers.
Bore: 50 mm
Stroke: 36 mm
Exhaust opening: 96 degrees (168 duration)
Transfers opening: 125 degrees (110 duration)
Intake opening: 80 degrees (160 duration)
I have a good buddy up in Cincinnati. He is a fantastic machinist, as well as a big fan of fat-bottomed girls. We made a trip up to see him and he promptly milled the jug down 0.0295" and made a 0.020" pop-up for the piston. This brought our squish down to 0.020 and brought up the compression nicely. Also, the jug itself was not square to the crank case. It was off by a few thousandths on the axis of the hinge pin, causing the piston to rock slightly every time it went up and down. Nik, of course, corrected this flaw from the factory. Now things are tight and moving in alignment. Andre, Mike and Brad made it a point to stop by, and we had a mini-GTG just shooting the bull while everyone got pop-ups made.
Nik (FATGUY)
Jug and Piston:
Andre (Andyshine77) and Erick (Erick) shootin the bull (Sorry Mike, I didn't get any pics of you and your lovely bride):
Brad (blsnelling) excited about his new pop-up:
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