Update on the 066 ghost problem. :msp_unsure:
As mentioned before, it got a complete tear down with new seals & case gasket. The carb got fresh parts, too, even though the old parts were barely used.
It ran fine at first, but midway through the first cut, it seemed to lose torque, and then it had trouble idling. Something wasn't right.
I immediately called it quits and proceeded to do a leak test. It had a big leak, at the cylinder base and at the head (this has the 2-piece head). Tried snugging up the head bolts and one was spinning -- threads stripped ! ! ! :mad2:
Apparently that bolt had popped the threads out while the saw was running. :mad2: Mr. Murphy hasn't been cutting me any slack, lately.
Tried a heli-coil. I accidentally screwed it in too far and was forced to fish it out. Tried another heli-coil, it went in kattywampus and had to be fished out, too. By that time the helicoil threads were too far gone so scratch the helicoil. Mr. Murphy strikes again ! ! ! :mad2:
No problem, I could tap the hole for 5/16-24 and make an homemade insert out of 5/16-24 rod. Except, the only 5/16-24 rod on hand was 18-8 stainless which is a bugger to tap. Broke my only 6 mm tap. Argh ! ! ! :mad2:
OK, ordered more taps and a chunk of carbon steel 5/16-24 rod. It showed up today. Made a purty insert and screwed it in with a couple of drops of red loctite so it shouldn't go anwhere.
Why did the threads strip out in the first place ? Thread engagement was 11mm, compared to 10mm on OEM bolts. But, to be safe, I made some studs out of 6mm all thread that provide about 20mm thread engagement.
New stud on top, old bolt on bottom.
It passed leak test with flying colors (0.72 inHg per hour) and seemed to run fine when I fired it up. Idled steady, and held steady RPM at WOT, though I did notice the H screw is very sensitive -- maybe a bigger main jet would reduce sensitivity ?
Will take it to the woods tomorrow and see if the ghost problem returns.
I did pick up a used WJ69, just in case, but will save it as a last resort, since I can't find anything wrong with the original carb.