Cllyde I have a newer 3120 I use for milling. I was concerned about the stress put upon it, it seemed to run lean and even apperared to vapor lock a couple of times after a long cut and rest/restart. I followed the advise of another and drilled the main jet out two numbered drill sizes larger. Have not had another vapor lock. I also removed the inner baffle tube in the muffler and slightly increased the outlet opening using a unibit. Actualy I drilled the opening utill the end of the inner baffle tube weld was gone which allowed the inner baffle tube to be removed. (prior to this I had to reach thru the opening that mates to the exhaust port and saw the other end of the baffle tube free with a hacksaw blade, somewhat time consumer cause you cant get a very long stroke in there) I also pryed the louvered outlet cover slots to a less restrictive postion but left the screen in place. The difference was a somewhat louder saw that would then "four stroke" coming out of the cut like a good saw should. Seat of the pants seemed to suggest it reved quicker. Now as for milling where the saw runs much more heavly loaded I cant say for sure that it felt as if it pulled any better. I have since welded into the muller outlet beneath the screen a short section of tubing to more closely match the stock opening sans the baffle tube. I think I may try a stock muffler again with the rejetted carb in light of the low rev/hi load nature of milling ,but for sure the larger main jet size lets the say run cooler. I can say for sure that the muffler mod seemed to allowed the saw to scavenge a richer mix as the saw would give that "four stroke" tone when reved no load prior to the gov taken over. This is somewhat un scientific but follows a logical approach based on current epa engineering of the newer saws. Hope this helps, bman