I finally got things together enough for the first test run! The mill actually runs and ripped the (too dry) log! While there still a things to do I'm quite happy to have gotten this far.
In my eagerness to test it I overlooked the importance of securing the log. It moved a lot during the cut and the beam turned up quite crooked. Log clamps similar to Norwoods Portamill PM14 are lined up for welding next.
Second, it gets very heavy to push the saw after a while. But a feed of some kind is coming, that's the reason for this thread after all.
I don't have much reference, but milling speed was a bit slower than expected. It might be due to very dry wood, too high rakes or that the log kept moving around. More tests are coming.
As you can see in the pictures, fresh paint really makes a difference. Everything but the bar and chain are repurposed pieces or from scrap metal. Especially the motors look very fresh now.
The oiler is gravity fed, with a 24V pneumatic valve that is controlled from the main motor VFD. When the saw turns on the valve opens. The normal bar chain oil was a bit too thick to flow well, but vegetable raps seed oil works fine.
The oil nozzle on the bar mount is made from an M8-screw that I turned to size and bored on my lathe. I managed to get hold of a ca 1910 Bradford engine lathe which has proven very useful for everything from making oil nozzles to wheel axle shims and washers. (There is a good picture of the same model here
https://doit101.com/Lathe/chapter1.html)
I've also had time to experiment with the iNVT VFDs and realized that I don't need the fancy control box with microcontroller. I made a new one with just the minimum of buttons, start, stop, up, down, left, right and emergency stop.
Again, a big thank you all for valuable input!
Stay tuned for more!