Canadian Cutter
ArboristSite Lurker
Hey folks, thought I might reach out for some help.
Got an old Homelite Blue XL-12 on the side of the road (fall clean up) she looked well taken care of .. everyone says these old girls are worth fixing , if the piston / rings look good.
- good spark
- removed the muffler, piston rings look good, good compression
- removed the flywheel, completely cleaned the points (carb cleaner) and the white piece of paper pulled through the points several times til clean (I didnt check the points gap or the timing)
- complete Tiliston carb kit installed very slowly / carefully ....... I adjusted the HI / LOW screws as per what most recommend (LOW unscrew 1 1/4, HI unscrew 1 full turn)
- everyone says the ignition coil rarely fails, so I just cleaned it
- Tested the condenser on a wood surface with the ohm meter, looks good
- the switch needed to be re soldered to the lead (done) but I havent actually tested the switch itself, might be worth replacing.
- will be replacing the fuel line and filter today (though they look good, filter is clean and line is supple with no cracks / leaks)
- plug has pretty good spark , maybe should be replaced none the less ?
she kicked and ran for 10 seconds when I brought her home with new gas but would not stay running ....... now after all the above work she still wont run, kicks every 3 or 4 pulls but wont fully start or run ? thoughts , maybe the condenser is bad ? maybe the points are bad ?
Got an old Homelite Blue XL-12 on the side of the road (fall clean up) she looked well taken care of .. everyone says these old girls are worth fixing , if the piston / rings look good.
- good spark
- removed the muffler, piston rings look good, good compression
- removed the flywheel, completely cleaned the points (carb cleaner) and the white piece of paper pulled through the points several times til clean (I didnt check the points gap or the timing)
- complete Tiliston carb kit installed very slowly / carefully ....... I adjusted the HI / LOW screws as per what most recommend (LOW unscrew 1 1/4, HI unscrew 1 full turn)
- everyone says the ignition coil rarely fails, so I just cleaned it
- Tested the condenser on a wood surface with the ohm meter, looks good
- the switch needed to be re soldered to the lead (done) but I havent actually tested the switch itself, might be worth replacing.
- will be replacing the fuel line and filter today (though they look good, filter is clean and line is supple with no cracks / leaks)
- plug has pretty good spark , maybe should be replaced none the less ?
she kicked and ran for 10 seconds when I brought her home with new gas but would not stay running ....... now after all the above work she still wont run, kicks every 3 or 4 pulls but wont fully start or run ? thoughts , maybe the condenser is bad ? maybe the points are bad ?