Loctite 620 would seal the metal to metal outer ring of an oil seal to the seal bore, with the engine under vac the green will be drawn in to any gaps.
Well it’s got a new seal now. I’ll check it tomorrow and see if it has any leaks.I was going to say that little leak was not causing a problem. I would also have put some sealant around the leak and applied vacuum to pull it into the crack and let it cure. Hopefully, no leaks now. Too bad you don't have another Tilly HL to try.
I’ll keep that in mind for the future.Loctite 620 would seal the metal to metal outer ring of an oil seal to the seal bore, with the engine under vac the green will be drawn in to any gaps.
Is the felt filter in the sediment bowl a new one or older used possibly hardened or partially blocked?. We replaced them every time we removed the glass for cleaning, about once a month back when those saws were our main tools in the woods. I think they came in a bag of 25 from our local dealer.Well it’s got a new seal now. I’ll check it tomorrow and see if it has any leaks.
So that leak wouldn’t cause a problem then? I figured since I found it I might as well fix it.
What’s your take on what the issue is? Carb related still?
I might try popping the Welch plugs off to see if there’s any crud in there.
What about that felt filter in the sediment bowl? Maybe I could remove that just to see if that’s restricting fuel flow?
It really does sound like it’s starving for fuel though. If it had an air leak wouldn’t it just run like that forever? It dies out like it ran out of fuel.
It’s the old one that came with the saw. I soaked it in chem dip but maybe it’s just too far gone? I couldn’t find any online at the time so I just left it.Is the felt filter in the sediment bowl a new one or older used possibly hardened or partially blocked?. We replaced them every time we removed the glass for cleaning, about once a month back when those saws were our main tools in the woods. I think they came in a bag of 25 from our local dealer.
Sounds like a problem I had on my boat. It idled fine and was ok at low speed but any high and it starved. Fuel filter in the carb was clogged - happened very suddenly. By all means, get that felt out and try it.It’s the old one that came with the saw. I soaked it in chem dip but maybe it’s just too far gone? I couldn’t find any online at the time so I just left it.
I could remove it temporarily just to see if it makes any difference. I’ve got a new filter in the tank so that should stop most of the crud from getting through.
Ok I’ll keep that in mind. Not sure if I’ll get to mess with it today, maybe tomorrow.I noticed in the video, when you loosened the fuel cap to see if that was causing fuel starvation, you tightened in right back up. You might want to try that again with leaving the cap loose for a few minutes. it takes a little while for the carb to recover the fuel volume under the diaphragm after it's been seriously depleted.
Agree with this recommendation. Weak spark can't keep up with fuel load & can be confused as carb issue.Should add, when it was running poorly with a bad condenser, one in a while it would pick up speed and sound normal, but drop out again. Electrical problems are funny that way.
Your post #124, Feb 24th; disassembled carb bits look correct, but #125 post.. what is the image of black plastic metering lever. Hopefully just some needle leak test setup. That needle lever seems weird / incorrect.
Cool, I'll keep that in mind. I guess it could be a small leak from the Mityvac itself. Either way, that small of a leak is not causing the issue, but I hear what you're saying.Looks like you have everything covered. One other thing I do on the vac/pressure test - if I see a drop, I pinch off the line going to the gauge. If it still drops, you have a leak in the gauge or the tubing.
I see. I sure hope it's just ignition related. I would love to replace the condenser and fire it up and have it run properly.Helped a friend today work on a sandcast poulan. Had good spark, apparently, but ran poorly, had to hold the trigger wide open and it barely ran. Let go and it would die. Spitting unburned fuel out of the exhaust. Turned out to be a bad condenser. After that was fixed, had trouble with tuning, not wanting to idle. That turned out to be a bad gasket for the reed valve plate and possibly a poor fuel filter. Remember, these things are 60 years old. Take nothing for granted.
That's how mine sounds. The idle fluctuates and my first instinct was to think that was related to an air leak or fuel starvation issue. But if the spark is inconsistent/intermittent, that would cause it to run funny as well.Should add, when it was running poorly with a bad condenser, one in a while it would pick up speed and sound normal, but drop out again. Electrical problems are funny that way.
Agree with this recommendation. Weak spark can't keep up with fuel load & can be confused as carb issue.
Assume you've followed others work. Samish Saw covers 2 quick looks at 620 Condenser & Carb rebuild.
As previously stated here, I've used Sig-01 Ignition Chip on Homelite. Samish did a clever trick of poking the chip terminal put thru gutted point grommet. Nice job!
Also, I can't erase my visual question on an earlier post.
Your post #124, Feb 24th; disassembled carb bits look correct, but #125 post.. what is the image of black plastic metering lever. Hopefully just some needle leak test setup. That needle lever seems weird / incorrect.
Edit (update) -- found the offset bracket CPM-01 chip shown by Samish. Less common than Sig-01 (Rotary 9334) or BM-11 versions.
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