Hedgerow
HACK
Did you ever get a measurement of the squish?
Just curious what it was...
Just curious what it was...
Nah, I didn't bother, partly because it's a clamshell engine and changing it would have required adding material to the piston. I don't have any way to do that. It would have been interesting to know though.Did you ever get a measurement of the squish?
Just curious what it was...
Well, kinda disappointing so far. It will run hard if I keep the revs up, but it has little torque if I bog it. If I push it a little the revs drop and it "4-strokes" like crazy. Now I know I don't have the tuning right yet, but I think the problem is low compression.
This was not a great P&C, rather a crappy one I was trying to clean up. After trying it for most of a tank I checked the compression (as best I could with my lousy gauge) and pulled the muffler and plug to look in. I only got 115psi. Things don't really look too awful in there - there are a couple of shiny section forming on the ring edge, and corresponding polished stripes on the cylinder wall over the exhaust port. They're not grooves, just polished, but it indicates the ring is not seated everywhere yet and must be riding on those high spots.
Just for grins I tried the other flywheel with less spark advance, and that didn't help at all.
I'm going to run it for a while until the ring seats (which may take longer if it's not that regular a surface), play with the tuning and see what happens. It actually runs pretty well if the revs stay up.
Can you video it at full throttle in and out of the cut?
That would take some time to put together. I tried tuning it in the cut, and it wanted the H much leaner than I had it set no load. Ran much better that way, and that's consistent with it being too rich. But it didn't sound too rich!
I didn't have enough time to work with it any more and I know it's not right yet. I have to put the other flywheel back on and try again. It may be that tuning is really the main problem.
The coil isn't rev limited, it's a pretty simple saw. I did the initial tune so it sounded like it was 4 stroking no load. Tried it a couple of times wide open, enriched the H until I just got a bit of that blat sound. But that seems way too rich in the cut. I wasn't comfortable leaning it too much though. I need more time and was rushed because we had somewhere to go. Of course there is only an L and H adjustment, and it seemed like it would pull well at revs but if it got down in revs it would get stuck and sounded very rich. When I tuned it in the cut I was able to get it to pull better by leaning it.
Too many beers tonight and I'm not being clear - what I felt was appropriate no-load seemed way too rich in the cut when the revs dropped, but what pulled better in the cut didn't sound like it was 4-stroking no load.
I'm a little concerned that the compression is low but that at higher revs it holds cylinder pressure better - but I need to just take a little time and work through the tuning first.
I did learn something very important though - if you get a hole in your jeans just below the crotch on the right leg, your pants leg will fill up with chips. This can be uncomfortable.
Thanks - the muffler was opened up before I started this phase of the project. Also, I realize the plating is thin, which is why I stuck with 400 grit, and it looks like the plating is intact.WHW, Good Job! Hope you gutted the muffler to help it breath.
Also, be careful with any hone on a plated cylinder. The plating is really thin, measured in microns, so its too easy to ruin a cylinder. If a cylinder is scored badly above the exhaust port, any acid you apply will get between the plating and the cylinder and render it useless too.
Well, so much for the PP315 engine. It ate a circlip and it is no more! I was noodling some knotty persimmon, and running it hard, and it was working very well. Then I heard a faint click and it quit, and I could tell that was all she wrote. I pulled it apart and found the lunched circlip, but I'm at a loss as to why. Shame too, as the cylinder was looking really nice and clearly the ring was seating better.
I'm going to start a new thread to try to figure out what happened.
It was in the groove. Based on discussions in this thread: http://www.arboristsite.com/chainsaw/206965.htm I've come to the conclusion that the clip did not have the proper tension. That left it loose and it simply pounded itself and the groove, until it either broke or got loose enough to pop out.
Now I just have to decide if I'm going to port the 46cc engine before I put it in or not. It ran very well just the way it is, but I'm still deciding.
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