tex
ArboristSite Operative
Here is the background...
Picked up a ms660 mag about a year ago with a burned up top end. Before tearing the saw down, I did a vac check on the case. All ok. I installed an NWP big bore top end. Tuned the carb all the out (rich) to the stops. Saw ran good like that, so I never played with it further. Ran the saw on and off through the summer with no problems, other than I thought that a 98cc saw shouldn't be able to be bogged with only a 25" bar.
So, I did a muff mod.
for the muffler mod, I drilled two 1/2" holes in the baffle, and one 3/4" hole out the front cover with a fabbed deflector. The screen I put inside is large enough that it is not restrictive to the flow. All said and done, I've added a 3/4" hole in addition to the stock hole for exhaust flow.
I pulled the limit caps off the carb, and started with 1/2 turn out on the low, and 1 1/2 turns out on the high (double the factory settings). The saw wouldn't start, so I increased the low setting to about 1 full turn before it would start. With the saw now running, I opened the low mixture trying to get it to 4 stroke. It never really did 4 stroke, but did slow down. I then leaned it to find my highest rpm which was at about 3/4 of a turn. I richened it from there back to 1 turn open, and then moved to my high mixture. I revved the saw to wid open, and began opening the mixture. Like on the low side, it never really 4 stroked, even at 3 full turns out on the screw. I let it back down to idle, and checked my low setting again with the same procedure, and ended up back at 1 turn out. Went back to the high side, and still couldn't get it to noticably 4 stroke. Changing the mixture did change its responsiveness when i'd blip the throttle, but I couldn't really get it to slow down by richening it up.
Long story short...the last time I let the throttle down, was the last time. Its seized tight...still.
Did I do something wrong with the tuning, does the carb need to be gone through, did I go too far on the exhaust, did the big bore kit have anything to do with it?
Any input would be greatly appreciated.
Picked up a ms660 mag about a year ago with a burned up top end. Before tearing the saw down, I did a vac check on the case. All ok. I installed an NWP big bore top end. Tuned the carb all the out (rich) to the stops. Saw ran good like that, so I never played with it further. Ran the saw on and off through the summer with no problems, other than I thought that a 98cc saw shouldn't be able to be bogged with only a 25" bar.
So, I did a muff mod.
for the muffler mod, I drilled two 1/2" holes in the baffle, and one 3/4" hole out the front cover with a fabbed deflector. The screen I put inside is large enough that it is not restrictive to the flow. All said and done, I've added a 3/4" hole in addition to the stock hole for exhaust flow.
I pulled the limit caps off the carb, and started with 1/2 turn out on the low, and 1 1/2 turns out on the high (double the factory settings). The saw wouldn't start, so I increased the low setting to about 1 full turn before it would start. With the saw now running, I opened the low mixture trying to get it to 4 stroke. It never really did 4 stroke, but did slow down. I then leaned it to find my highest rpm which was at about 3/4 of a turn. I richened it from there back to 1 turn open, and then moved to my high mixture. I revved the saw to wid open, and began opening the mixture. Like on the low side, it never really 4 stroked, even at 3 full turns out on the screw. I let it back down to idle, and checked my low setting again with the same procedure, and ended up back at 1 turn out. Went back to the high side, and still couldn't get it to noticably 4 stroke. Changing the mixture did change its responsiveness when i'd blip the throttle, but I couldn't really get it to slow down by richening it up.
Long story short...the last time I let the throttle down, was the last time. Its seized tight...still.
Did I do something wrong with the tuning, does the carb need to be gone through, did I go too far on the exhaust, did the big bore kit have anything to do with it?
Any input would be greatly appreciated.