The red loctite didn’t hold. I was able to torque the bar stud up to a max of 14 ft lbs, but it actually required 17. Started to spin at 15.
upon inspection I can only presume the slightly wallowed out threads in the mag didn’t squeeze the air out enough for the red loctite (263) to fully hold.
Had a chat with some of you on here I weighed up my options. Finally I settled on new cases. I was able to get them from my dealer for 130 aussi dollars. After leaving the shop it clicked that these newer cases would have the flipping cap and so I canceled the order.
Then went back and looked up stairs at their spare parts boxes and found two 034’s. figuring that the front adjuster is the only noticeable difference, it would still work.
Got home and found there were a number of slight variances. I weighed up options back and forth and decided to return the cases.
I finally decided to use JB weld to lock the sleeve in place. This morning I torqued the bar nuts up to 17 ft lbs to see if it would hold, it did twice.
I want to keep the build an 034 super so it’s the way I’m going to go forward.
Just took the carby apart and Welch plug out before sticking it in the ultrasonic cleaner.
Worth noting, Harley and DND were right, the 411 PN is correct for the nozzel. The 1125 ending in 08 has a drilling in the top and is not right.
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