After removing it to replace the oil seal the spark is weak. It was fine before. Connections look good. It's weak through an inline spark tester that works good. Any ideas?
This is the cap that I used. Im no electrical engineer. Is it possible I wired it backwards? Im not getting much feedback on this thread so I'll use it to think out loud. Thank you to all that have helped so far. These ignitions are a pain.
https://www.ebay.com/itm/0-01uF-400...-c624cbbff582&epid=5006985344&redirect=mobile
I tried the foggy sail ignition trick and still have weak spark. I have another one that also had weak spark, i stole the coil off of it just to try and still had weak spark. I tried with the switch disconnected and changed the plug wire. I also tried a different rotor. Proline offers an aftermarket for $130. Thats a lot of bread. Does anyone have any idea what to try? I have a decent amount of money and a ton of time in this thing the experience is usually a lot of fun for me but I'm getting tired of looking at it.
They can be a pain. I made a homeaid puller and used a heat gun. I replaced the seals and rings on all of them when I was done as well as a gasket delete on one and thinner gasket on another. I now have two running and this third Im working on. I plan on milling to make a little side money. We have a stump dump here on the farm and the tree guys are constantly dumping good firewood as well as stuff good for milling.I wish I had something to offer more than this.....
If it makes you feel any better, I've had zero luck getting the inner flywheel off a spare unit/case, LOL!
They can be a pain. I made a homeaid puller and used a heat gun. I replaced the seals and rings on all of them when I was done as well as a gasket delete on one and thinner gasket on another. I now have two running and this third Im working on. I plan on milling to make a little side money. We have a stump dump here on the farm and the tree guys are constantly dumping good firewood as well as stuff good for milling.
My solution for the problem you are having was/is I got 3 good hard bolts (Like 8 grade in SAE only the metric equivalence) with a nut for each. With a flat face puller with 3 symmetrical slots have a flat washer against the bolt head through the puller (with the 3 bolts in in the puller) thread the nut on the bolt then thread the bolt into the flywheel where it is threaded for the Fanwheel.(all 3 equally) Run the nut down (Jamb) to lock it in place this gives you 3 legs to pull with that hopefully won't pull the threads out. Center and pull as evenly as possible. I haven't had to use heat yet but tempted a few times. Some of the earlier flywheels had smaller holes threaded into them to hold the fan wheel on than the later version Bosch and I did pull (Ruin) a thread once and oversized/rethreaded it just keep in mind where the module and coil are so you don't bugger them. A good straight rap with a hammer on puller when under load will help a lot. Good luck.I wish I had something to offer more than this.....
If it makes you feel any better, I've had zero luck getting the inner flywheel off a spare unit/case, LOL!
Wish I could post Pictures. That is what my first puller looked like .. I had longer bolts so I could jamb the nuts against the flywheel 'cuz my firs flywheel was the smaller bolts holding the fan wheel. and I was really worried about stripping it. I didn't need heat and seals weren't readily available to me at the time.This is the puller. I don't know how I'd done it without it.
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