I proceeded slowly and in multiple steps taking care to test each phase thoroughly with several tanks of gas, kept in good tune, and loaded up in big wood.
First I just reamed out the two existing slots and opened up around the deflector shield exit a good bit, this did very little for performance and the exhaust note hardly changed.
Next I drilled a 5/16" hole in the indented area of the muffler directly inline with the exhaust port which bypasses the internal baffle, surprisingly the increase in throttle response was obvious, running good, sound still well under my Db tolerance.
Today I took a rat file to the 5/16 hole and made it into a slot. Outstanding throttle response, pulls chain alot faster under load, sounds cool with a good "pop-pop" at idle and a tolerable Db at WOT.
I ran two tanks today with a goofy grin on. It sounds and runs so different I decided to pull the plug to make sure I had the carb dialed in right. There's more tan than what this pic shows but it's still whiter than I've ever seen it.
Threw a new NGK in it and opened the H screw just a sniggle, cleaned her up and took pics
Here you can kinda see the increased size of the exhaust exit
Good-looking 10 year old boat anchor
First I just reamed out the two existing slots and opened up around the deflector shield exit a good bit, this did very little for performance and the exhaust note hardly changed.
Next I drilled a 5/16" hole in the indented area of the muffler directly inline with the exhaust port which bypasses the internal baffle, surprisingly the increase in throttle response was obvious, running good, sound still well under my Db tolerance.
Today I took a rat file to the 5/16 hole and made it into a slot. Outstanding throttle response, pulls chain alot faster under load, sounds cool with a good "pop-pop" at idle and a tolerable Db at WOT.
I ran two tanks today with a goofy grin on. It sounds and runs so different I decided to pull the plug to make sure I had the carb dialed in right. There's more tan than what this pic shows but it's still whiter than I've ever seen it.
Threw a new NGK in it and opened the H screw just a sniggle, cleaned her up and took pics
Here you can kinda see the increased size of the exhaust exit
Good-looking 10 year old boat anchor