jerseyjeff
ArboristSite Member
I put this in the wrong place, and need to delete the post in the manual thread.
After Sandy I realized that I needed a bigger saw to go with my little redmax 4500, and I stumbled on a dolmar/makita 6400 at Home Depot for 100, and picked it up. I discovered the piston was installed backwards, and the off switch was more of a suggestion, but, in general it has turned out to be a nice saw, and it is very light, and will run a 20-24 inch bar all day. My buddy had an NWP piston kit and I could not resist turning it into an 84 cc saw. After putting in the kit, checking compression (127 psi) I fired it up without a bar, and then discovered the e-clip was missing when the drum fell off, and the clutch went into low orbit. Oops.
I replaced the the clutch, drum, sprocket and needle bearings, and a brandy new e-clip too. The saw ran great, and pulled like mad. I did a few test cuts in some 6 inch oak (all I had) and was happy.
I read about the HD filter kit and liked the idea of additional filtration, and ordered one up, put the black humpback on the saw, a new bar and chain, and headed up to my in laws to drop a bunch of ash (yeah ash borer). The saw started on 1/4 choke, went straight to WOT, and revved a little and then stalled. I could not get the saw to run on or start on anything less than 1/2 to 1/4 choke, and it went from full speed to off. I ended up running 8 tanks of gas through the redmax this weekend, and it handled everything like a champ, but the teal paper weight is making me a bit grumpy.
I am thinking I may have a carb issue based issue based on reading the old threads, and my plan is to start messing with the L screw, but, because I only know enough to be dangerous, I wanted to ask before I make it worse.
After Sandy I realized that I needed a bigger saw to go with my little redmax 4500, and I stumbled on a dolmar/makita 6400 at Home Depot for 100, and picked it up. I discovered the piston was installed backwards, and the off switch was more of a suggestion, but, in general it has turned out to be a nice saw, and it is very light, and will run a 20-24 inch bar all day. My buddy had an NWP piston kit and I could not resist turning it into an 84 cc saw. After putting in the kit, checking compression (127 psi) I fired it up without a bar, and then discovered the e-clip was missing when the drum fell off, and the clutch went into low orbit. Oops.
I replaced the the clutch, drum, sprocket and needle bearings, and a brandy new e-clip too. The saw ran great, and pulled like mad. I did a few test cuts in some 6 inch oak (all I had) and was happy.
I read about the HD filter kit and liked the idea of additional filtration, and ordered one up, put the black humpback on the saw, a new bar and chain, and headed up to my in laws to drop a bunch of ash (yeah ash borer). The saw started on 1/4 choke, went straight to WOT, and revved a little and then stalled. I could not get the saw to run on or start on anything less than 1/2 to 1/4 choke, and it went from full speed to off. I ended up running 8 tanks of gas through the redmax this weekend, and it handled everything like a champ, but the teal paper weight is making me a bit grumpy.
I am thinking I may have a carb issue based issue based on reading the old threads, and my plan is to start messing with the L screw, but, because I only know enough to be dangerous, I wanted to ask before I make it worse.