drf255
BAD CAD
Got into the jug last night. It's very difficult to get a pic of the cylinder ports on a clamshell. The angle makes it nearly impossible to get anything worth looking at. The jug is nearly 4" deep.
I used a piston ring as a guide. Scribed sharp lines with a sharpie and went to work.
I may have raised the exhaust a degree or 2 in error. The ports were widened by around 20%. Visually MUCH wider than stock. Plenty of meat left to keep the rings seated.
I blended the ports to the openings. After I was done, I took a small spherical stone and went around the port inside the cylinder. There was a definite ridge at first which I knocked down.
The combustion chamber on this Huztl jug appears smaller than on OEM. The OEM jug has a bit of opening coming back to the intake side, this has none.
I did notice that the piston height (from the top of the wrist pin to the top of the piston) was lower than OEM. I'm wondering if this is why compression runs generally lower on these AM P&C kits. Looks like it would be a safety issue for their parts.
I tried welding a dome on a burnt out piston. I think I did too much. The biggest problem was how dirty the old OEM casting was. Even after SS brushing and acetone, a lot of black soot. The cleaning action of the AC wave pitted the piston around the dome a bit.
I purchased the 4xxl tig cups.
I wish I could get some pics. I took a few, but so hard to appreciate anything.
I used a piston ring as a guide. Scribed sharp lines with a sharpie and went to work.
I may have raised the exhaust a degree or 2 in error. The ports were widened by around 20%. Visually MUCH wider than stock. Plenty of meat left to keep the rings seated.
I blended the ports to the openings. After I was done, I took a small spherical stone and went around the port inside the cylinder. There was a definite ridge at first which I knocked down.
The combustion chamber on this Huztl jug appears smaller than on OEM. The OEM jug has a bit of opening coming back to the intake side, this has none.
I did notice that the piston height (from the top of the wrist pin to the top of the piston) was lower than OEM. I'm wondering if this is why compression runs generally lower on these AM P&C kits. Looks like it would be a safety issue for their parts.
I tried welding a dome on a burnt out piston. I think I did too much. The biggest problem was how dirty the old OEM casting was. Even after SS brushing and acetone, a lot of black soot. The cleaning action of the AC wave pitted the piston around the dome a bit.
I purchased the 4xxl tig cups.
I wish I could get some pics. I took a few, but so hard to appreciate anything.