I tapped and rapped and gave a few hard whacks and didn't budge it. In an act of desperation I put a plastic hammer on top of the threaded part and put a deep socket over the bearing race on the other side, got both sides to perfectly .030 but as soon as I let the press off it went back how it was before. When I first got the halves together they where both .035, but when I torqued the bolts down the one side came in to .025 while the other side stayed at .035. I'm done fooling with it tonight, may take it to the station with me tomorrow to mess with it in my downtime. I'll give the nut and washer trick a try. My shift partner used to be my mechanic so maybe he can offer some insight as well.