skids-stihls
ArboristSite Lurker
Hi there Arb team.
So after finishing my tacho mounting mission Featured here https://www.arboristsite.com/threads/my-easy-tacho-mount-“i’ll-show-you-mine-even-if-you-haven’t-shown-me-yours”.361956/
I was going over the MS270 again to write down some reference rpm and screw turns after the muff mod. I’d also had enough of a break in the weather to bring a ring of wood into the barn so I can tune in the cut regardless of weather and time of day.
I was able to (several times) have it idling ok, great response (no bog) from idle to WOT, and had it sounding pretty good in the cut around 9500-10000, which gave a max rpm of around 13,600-13,700 without load.
However the idle kept changing and with each adjustment I had to change the H screw too if keeping to similar rpm and good response.
I also thought that the L adjustment seemed to alter the speed at a slower rate than I’d have expected. Eg turn a little, then wait for reaction rather than slowly turning and listening/watching. Then after a cut, it would change again. I topped up fuel once warm as I hadn’t checked the fuel hose for leaks in the tank end yet, still the same. I also thought it was taking a while to get back to idle after WOT or a cut, (slowing down but not instant).
Anyway, I got it to a stage where I was happy enough to put it into Dads box of tricks for his task tomorrow, so he can blunt his 026, then my 270 and I’ll sharpen both at lunch time, more cut time for him. But then I decided to do one more rip(with the grain) on the bluegum ring, plenty of grated cheese coming out and still around 9500-10,000 rpm in the cut, lift a little and 4 stroke, into it again and cleared up, cut well.
Then I backed up ready for a brief idle down before refuel and into the toolbox, “CLICK, CLACK, CLUNK, and STALL”
I couldn’t move the pull cord
I was sure revs were low enough to not be too lean, so back to the workshop and pull plug, looked as ok as I could tell since it’s not new or just been set for a read. Pulled the muffler, piston up position but oily enough and no scoring, pulled starter cover and moved flywheel by hand, it only moved a knats kiss each way, but the piston moved with it. So off with the flywheel and thank goodness, problem found, (the dreaded loose bolt hitting the flywheel) pretty pleased it happened at idle rather than WOT,
The other 2 were still tight but the one that hit the Flywheel had a bend in it. Not bad but enough to not reuse it, not now that I’m all the way in here anyway.
Now for my dumb question, the hole is very deep compared to the bolt, does this go right through to the crank case? or would the air leak symptoms be from the case not being clamped together with only one bolt missing? The only reason it matters is because while replacing the bolt, I plan to locktite them and need to know just how careful I need to be with the locktite, obviously if a drip could make it to the crank case then I’ll need to be more sparing with the locktite and probably sit the saw on its bum while fastening them just to be safe.
Or if the locktite is just a bad idea in that area and occasional flywheel removal to check them is better, then I’m ok with that, just seems this is the most likely place to find someone who knows that.
Anyway hopefully once together this sorts the L speed issues, sorry for the long explanation, but sometimes more is more.
Be safe out there folks.
So after finishing my tacho mounting mission Featured here https://www.arboristsite.com/threads/my-easy-tacho-mount-“i’ll-show-you-mine-even-if-you-haven’t-shown-me-yours”.361956/
I was going over the MS270 again to write down some reference rpm and screw turns after the muff mod. I’d also had enough of a break in the weather to bring a ring of wood into the barn so I can tune in the cut regardless of weather and time of day.
I was able to (several times) have it idling ok, great response (no bog) from idle to WOT, and had it sounding pretty good in the cut around 9500-10000, which gave a max rpm of around 13,600-13,700 without load.
However the idle kept changing and with each adjustment I had to change the H screw too if keeping to similar rpm and good response.
I also thought that the L adjustment seemed to alter the speed at a slower rate than I’d have expected. Eg turn a little, then wait for reaction rather than slowly turning and listening/watching. Then after a cut, it would change again. I topped up fuel once warm as I hadn’t checked the fuel hose for leaks in the tank end yet, still the same. I also thought it was taking a while to get back to idle after WOT or a cut, (slowing down but not instant).
Anyway, I got it to a stage where I was happy enough to put it into Dads box of tricks for his task tomorrow, so he can blunt his 026, then my 270 and I’ll sharpen both at lunch time, more cut time for him. But then I decided to do one more rip(with the grain) on the bluegum ring, plenty of grated cheese coming out and still around 9500-10,000 rpm in the cut, lift a little and 4 stroke, into it again and cleared up, cut well.
Then I backed up ready for a brief idle down before refuel and into the toolbox, “CLICK, CLACK, CLUNK, and STALL”


I was sure revs were low enough to not be too lean, so back to the workshop and pull plug, looked as ok as I could tell since it’s not new or just been set for a read. Pulled the muffler, piston up position but oily enough and no scoring, pulled starter cover and moved flywheel by hand, it only moved a knats kiss each way, but the piston moved with it. So off with the flywheel and thank goodness, problem found, (the dreaded loose bolt hitting the flywheel) pretty pleased it happened at idle rather than WOT,
The other 2 were still tight but the one that hit the Flywheel had a bend in it. Not bad but enough to not reuse it, not now that I’m all the way in here anyway.
Now for my dumb question, the hole is very deep compared to the bolt, does this go right through to the crank case? or would the air leak symptoms be from the case not being clamped together with only one bolt missing? The only reason it matters is because while replacing the bolt, I plan to locktite them and need to know just how careful I need to be with the locktite, obviously if a drip could make it to the crank case then I’ll need to be more sparing with the locktite and probably sit the saw on its bum while fastening them just to be safe.
Or if the locktite is just a bad idea in that area and occasional flywheel removal to check them is better, then I’m ok with that, just seems this is the most likely place to find someone who knows that.
Anyway hopefully once together this sorts the L speed issues, sorry for the long explanation, but sometimes more is more.

Be safe out there folks.