Wright Reciprocating Saw, pics and overhaul inside....

Arborist Forum

Help Support Arborist Forum:

This site may earn a commission from merchant affiliate links, including eBay, Amazon, and others.

444

ArboristSite Lurker
Joined
May 10, 2018
Messages
34
Reaction score
93
Location
Canada
A couple years ago I picked up a Wright GS-5020A reciprocating saw. Not much tech info out there on these so I figured I would share what I can. After sitting for some time I finally spent some time on it and got the old gal overhauled. Air cleaner was missing so I had to make one although I wish I had the correct one. The blade is worn down a bit up front so I know she's got some miles on her. I would really like to find a new blade if anyone has one let me know.

I had it sitting for a long time doing nothing and one day I decided to fix the recoil rope and put my compression tester on it. I had good spark and it was really hard to pull over. The saw was jumping all around my bench. Pulled 85psi on the compression tester. I dumped some fuel in the tank to see what would happen. To my surprise it started and ran. It ran badly but it was proof of life. I put it back in the garage thinking I should take apart and measure it up for crank seals to see if I could find something. Fast forward another year of doing nothing with it and I find a guy on ebay selling a NOS Wright 632595 gasket set. The only documentation I had was a grainy half scan of a parts manual I found by searching online. The pictures seemed like this gasket set was a good match but I had no way to know for sure. For 10 bucks I took a gamble and bought it and to my surprise it was the correct kit for this saw!

This saw was a joy to work on. The casting and machining quality is top notch. Everything is easy to work on and it was fun because it's something different. It's 115cc, horizontally opposed 2 cylinder engine. The power cylinder is a 2.5" bore while the blade cylinder is a 1.25" bore. The blade cylinder doesn't have a spark plug, instead it has a shaft extending out the top of the piston that actuates the saw blade directly. The blade piston is on the opposing throw of the power piston so it doubles as a bit of a supercharger. I think that combined with the reed valve is why it runs so well even at only 85 psi. It starts super easy and I guess after having the juices flowing from doing some running and cutting it now pulls over quite easy. I have a cheapie ebay tach I bought many years ago temporarily mounted to it and she starts very easy and settles down to a smooth 2300rpm idle. Top RPM is governed to 5000rpm via a secondary throttle blade in the intake manifold. It's quite fun to cut with. I do have to saw it back and forth a bit while cutting to help clear the kerf or it slows down cutting speed. Vibration is not noticeable with a decent pair of work gloves. The trigger doubles as a kill switch by grounding out the coil so in order to idle you need to push the trigger to the left as you let off the trigger to place it into the idle detent which is the only thing I don't like about the saw other than it's 25lb weight! When cutting, the bar flexes more than I expected but worked great for cutting a tree stump off my yard right flush with ground level and I cut a bunch of firewood and have about 1.5hrs on it so far. I run it at the original 16:1 mix, lots of smoke at startup when on the choke but otherwise when cutting I don't notice it.
 

Attachments

  • 20180509_163748.jpg
    20180509_163748.jpg
    867.9 KB
  • 20180509_163723.jpg
    20180509_163723.jpg
    875.6 KB
Found an owners manual for a GS-5020 posted to the forestry forum to be a big help. Has some good tech info like how to set the ignition timing, point gap, spark plug type, etc.
 

Attachments

  • pg_1.jpg
    pg_1.jpg
    84.5 KB
  • pg_2.jpg
    pg_2.jpg
    102.4 KB
  • pg_3.jpg
    pg_3.jpg
    95.3 KB
  • pg_4.jpg
    pg_4.jpg
    101.6 KB
  • pg_5.jpg
    pg_5.jpg
    86.5 KB
  • pg_6.jpg
    pg_6.jpg
    90 KB
  • pg_7.jpg
    pg_7.jpg
    100.8 KB
  • pg_8.jpg
    pg_8.jpg
    63.5 KB
  • pg_9.jpg
    pg_9.jpg
    79.4 KB
  • pg_10.jpg
    pg_10.jpg
    120.6 KB
Scans of a different Wright owners manual, mostly a duplicate of stuff from the other owners manual I posted.
 

Attachments

  • scan0007.jpg
    scan0007.jpg
    78.6 KB
  • scan0008.jpg
    scan0008.jpg
    70.2 KB
  • scan0010.jpg
    scan0010.jpg
    68.4 KB
  • scan0011.jpg
    scan0011.jpg
    66.7 KB
  • scan0012.jpg
    scan0012.jpg
    74.3 KB
  • scan0013.jpg
    scan0013.jpg
    66 KB
  • scan0016.jpg
    scan0016.jpg
    63.9 KB
Crank case halves, here you can see the large ball bearings and the blade piston with the shaft that hooks directly to the blade. There were in like-new shape, I guess without the combustion gasses and pressure they don't take any wear. Had two piston rings just as beefy as those on the power piston.
 

Attachments

  • 20180219_173910.jpg
    20180219_173910.jpg
    510.6 KB
Cylinder head is unusual in that you have the exhaust port on one side and directly across from it a removable cover on the intake side. I wonder if this was done so the transfer ports could be drilled after the cylinder liner was pressed in? On a two stroke engine I can't imagine any other reason you would want access to the intake transfer ports. The original gasket for the cover was sucked partly into the intake transfers so it was leaking a little.
 

Attachments

  • 20180309_202536.jpg
    20180309_202536.jpg
    409.8 KB
  • 20180309_202644.jpg
    20180309_202644.jpg
    391.8 KB
Cylinder head reinstalled, reed valve pictured.
 

Attachments

  • 20180309_203919.jpg
    20180309_203919.jpg
    437.9 KB
  • 20180309_205257.jpg
    20180309_205257.jpg
    379.5 KB
trigger housing reinstalled.
 

Attachments

  • 20180317_125242.jpg
    20180317_125242.jpg
    424.9 KB
  • 20180317_125256.jpg
    20180317_125256.jpg
    410.9 KB
Ignition system is neat. It's a removable assembly that contains the breaker point, condenser and coils. It clamps onto a collar cast into the crank case halves and can be rotated to adjust timing. Note the scratch marks on the crank case and ignition stator assembly are original and referenced in the owners manual as how you ensure timing is set correctly. Removable cam lobe is keyed and slips onto the crankshaft.
 

Attachments

  • 20180317_130046.jpg
    20180317_130046.jpg
    418.9 KB
  • 20180317_130530.jpg
    20180317_130530.jpg
    433.7 KB
  • 20180317_131653.jpg
    20180317_131653.jpg
    296.4 KB
  • 20180317_132608.jpg
    20180317_132608.jpg
    427.5 KB
  • 20180317_132831.jpg
    20180317_132831.jpg
    379.2 KB
Trigger assembly is pretty simple. Has a push button you press in to engage the fast idle by propping up the trigger so you can pull start without having to hold the trigger. Flywheel and housing are pretty straightforward, crankshaft nut is reverse thread.
 

Attachments

  • 20180317_133057.jpg
    20180317_133057.jpg
    398.5 KB
  • 20180317_133731.jpg
    20180317_133731.jpg
    457 KB
  • 20180317_134037.jpg
    20180317_134037.jpg
    405.2 KB
  • 20180317_134507.jpg
    20180317_134507.jpg
    331.8 KB
  • 20180317_134448.jpg
    20180317_134448.jpg
    322.1 KB
  • 20180317_134836.jpg
    20180317_134836.jpg
    289.7 KB
  • 20180317_135731.jpg
    20180317_135731.jpg
    309.7 KB
Carter ND carb was pretty simple and in good shape. Surprised it even ran, the original fuel pump diaphragms were brittle and showed physical cracks. A replacement kit from sugar creek supply fit well. Fuel inlet needle is nylon or plastic and showed no wear. High speed fueling is adjusted with a thumbwheel where low speed and idle are by screwdriver.The only thing I don't like about the carb is the choke blade shaft flops around and is tensioned by the air cleaner screws. Since I had to make my own air cleaner housing the choke flapper wasn't tensioned right and would just flop open/closed. I took a hole puncher and punched a hole out of gasket material and shoved it into the threaded hole for the air cleaner screws and reassembled. It gives the choke shaft the proper amount of tension.
 

Attachments

  • 20180317_150029.jpg
    20180317_150029.jpg
    340.4 KB
  • 20180317_151022.jpg
    20180317_151022.jpg
    396.2 KB
Governor weights are held onto the end of the crank shaft by a small mild steel pin that was then peened into place. After getting it punched out I saw it was ruined both from my punching and being worn down where the weights pivot. I found a drill bit in my set of the exact right size, I cut it down and put a small blob of jb weld on each end to keep it into place. A cut down HSS drill bit does not peen very well to stay in place and this was the other other way that I though would work. Of course the governor plate has to be able to slide over top of where this pin goes as the weights move it in/out so it has to be a smooth repair. And without taking all that stuff off you can't change the crank seal on that side.
 

Attachments

  • 20180318_134222.jpg
    20180318_134222.jpg
    341.6 KB
  • 20180318_140450.jpg
    20180318_140450.jpg
    387.9 KB
  • 20180318_140843.jpg
    20180318_140843.jpg
    414.2 KB
  • 20180318_141813.jpg
    20180318_141813.jpg
    375.2 KB
  • 20180318_144626.jpg
    20180318_144626.jpg
    358.9 KB
Final reassembly. Bar was a bit corroded so I threw some paint on it just for corrosion protection. Later on I want to strip it and power coat it but I'm in the early construction phases of my powder coating oven and probably won't have that finished until winter.
 

Attachments

  • 20180318_152305.jpg
    20180318_152305.jpg
    300.8 KB
  • 20180318_152655.jpg
    20180318_152655.jpg
    385 KB
Back
Top